I didn't think Wen was still with us, but they're still a going concern with a website. I don't think they bother much, if at all, with the Canadian market; I never see their stuff around here.
While looking over their website, I learned that Wen Products was founded the same year as I was born -- 1951. And they still make this engraver. It's now the Model 21B. (Maybe the 'B' denotes an improved stroke adjustment screw.)[1]
In any event, this tool is well worth repairing. An engraver is good to have in the shop when you're dismantling an unfamiliar piece of machinery. You can use it to mark parts' relationships with one another to ensure that a thing goes back together exactly as it came apart. That can save a lot of aggravation at times.
Here's a view of the tool opened up. It's just two threading screws and a snap-ring to get it apart.
You can't really see it in the photo, but the nylon screw has had an unsuccessful repair attempt made on it in the past. That complicates things a bit because the screw's thread has been distorted at the broken end by the repair attempt. I don't have any 8-32 nylon screws on hand, so I'd really like to find a way to salvage that existing screw. What I have in mind is to use the female portion of a binder post (aka 'Chicago screw') to recreate a handle end on the screw remnant.
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And with some difficulty, that worked. Here's a shot of the finished screw repair, along with examples of Chicago screws.
The difficulty lay in cleaning up the screw's battered thread. An ordinary threading die was too thick to be workable. What I needed, in effect, was a very thin threading die that I could pass the screw remnant through to chase its thread. Since nylon is a relatively soft material, I was able to create an ersatz thread-chasing die from an ordinary 8-32 steel hex nut, like so.
Here's the engraver all back together in good working order.
I do think, though, that the adjustment screw's design was a bit marginal. It remains to be seen whether it will need further attention, and possibly a rework of some sort to improve it. Aside from that, it's a well-thought-out, well-constructed tool.
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SATURDAY, SEPTEMBER 3, 2011
Addendum
A reader in Australia informed me of something I was unaware of -- there's supposed to be a compression spring under the head of the stroke adjustment screw to keep it from wandering off its setting. The spring was long gone from the unit I had.
The Australian gentleman was of the opinion that the spring was awfully forceful for the screw. That may explain why the screw on my unit broke in the first place. As it's turned out, my adjustment screw has had so much abuse that it's now quite a snug fit in its nut, and stays put without a spring.
As I've said, the adjustment screw's design leaves a bit to be desired on what is otherwise a good tool.
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SATURDAY, NOVEMBER 26, 2011
Addendum II
I noticed that someone had been googling in search of a replacement tip for this tool. I'm afraid they're out of luck on that; Wen's website offers no replacement parts for any of their portable power tools.
It would be possible to remove the stylus and chuck it in a lathe for sharpening. Provided that the chuck can be locked onto the spindle so it can be safely run in reverse, you could ever-so-carefully present a counter-rotating hand grinder wheel to it, like so.
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And here's the outcome.
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Since I had the stylus out, I cleaned the spring and stylus and the stylus' ways and applied fresh grease. There's a synthetic grease known as 'STOS' that's excellent for fine mechanisms. It's expensive; the little 2 oz. tub pictured below set me back about twelve dollars.
Here's a way to get the stylus' spring compressed for reinstallation of the stylus in its ways; it's very difficult to do otherwise.
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SATURDAY, DECEMBER 10, 2011
Addendum III
I noticed something about the tool's operation that I don't much care for -- quite a lot of vibration is expressed at the head of the stroke adjustment screw when the tool is running. That's a source of needless noise, and it can't be good for the screw.
I suspect the reason for it is the way the stroke adjustment screw's nut is housed -- it's just a loose slip fit in its recesses. Epoxy can be put to use as a filler, even in places that need to be taken apart. I'm going to see if I can create a 'zero-lash' fit for the nut with epoxy, and see if that has any good effect on the tool.
Here's a close-up view of the nut in its right side recess. You can see that it has a fair bit of clearance in back of it.
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Here's the nut's recess sufficiently filled with slow-setting epoxy.
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There was a little bit of epoxy-fouling of the nut's thread; a chase with an 8-32 tap took care of that.
Now that I have the nut immobilized on one side, I have to do the same for the other side, while at the same time ending up with a casing that can still be taken apart. That's a little tricky.
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Here's a view of both casing halves just prior to assembly for fully bedding the nut.
It did work out, but not quite as I expected. Here it is opened back up after the epoxy had fully hardened.
Anyway, I appear to have what I was after -- a zero-lash fit for the nut that can still be taken apart. I'll take the two barrier screws out and clean up what squeeze-out there is under them.
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The nut's thread wanted chasing again -- there was a tiny bit of epoxy incursion. Here it is with the stroke adjustment screw back in place.
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Splendid! (There's a word you seldom see or hear anymore.) A splendid outcome.
The vibration at the head of the adjustment screw is now all but entirely suppressed. It's easier to adjust. I can't say that the tool is quieter, but it's smoother -- it no longer sounds like it's thrashing about inside.
So there we are. Epoxy is versatile stuff, and can be put to use in unorthodox ways to very good effect.
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Note -- SUNDAY, NOVEMBER 27, 2011
[1] I see that Wen has done a redesign. Their new engraver is the '21C', with a revised stroke adjustment. 'Took them long enough to get around to that.
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This is pretty cool, I have recently bought this same tool and it worked out for a while but eventually it stopped turning on I'm not Sure what happened. I'm planning on opening it up to see if there's something wrong with the motor or the cables connecting it. Thanks for this post it was informative
ReplyDeleteI really appreciate all your time and effort you put into this! Thank you. Very helpfull
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ReplyDeleteThis wasn't exactly what I was searching for, but you did surely (and right away) give the answer i was looking for! Man, you did a really fabulous and extremely informative post!!!...THINK I'LL BOOK MARK THIS :)
ReplyDeleteInstead of making all of those adjustments to the nylon screw I replaced it with a steel screw and placed two nuts behind the spring to be able to adjust the tension.
ReplyDeleteI have one of these, I found it today while searching for design inspiration for a miniature electric chisel. Thank you for saving me the trouble of dismantling it.
ReplyDeleteWere you able to find a way to insert a graver in the carbide rods place ?
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